特种油气藏 ›› 2021, Vol. 28 ›› Issue (6): 121-128.DOI: 10.3969/j.issn.1006-6535.2021.06.016

• 油藏工程 • 上一篇    下一篇

彩9井区西山窑组特高含水油藏CO2混相驱先导试验

张艳梅1, 万文胜1, 李琛1, 罗鸿成1, 刘衍彤2, 张会利1, 张瑞雪1   

  1. 1.中国石油新疆油田分公司,新疆 阜康 831511;
    2.新疆新易通石油科技有限公司,新疆 克拉玛依 834000
  • 收稿日期:2020-11-17 修回日期:2021-09-22 出版日期:2021-12-25 发布日期:2022-02-16
  • 通讯作者: 刘衍彤(1966—),女,高级工程师,1988年毕业于西南石油学院油藏工程专业,1998年毕业于该校油气藏工程专业,获硕士学位,现主要从事油气田开发、提高油藏采收率技术服务等工作。
  • 作者简介:张艳梅(1973—),女,工程师,1994年毕业于重庆石油学校石油及天然气开采专业,2007年毕业于西安石油大学工商管理专业,获学士学位,现主要从事提高油藏采收率研究、油田老区开发方案编制等工作。
  • 基金资助:
    国家科技重大专项 “新疆低渗透砾岩油藏CO2驱油与埋存先导试验”(2016ZX05056)

Pilot Test of CO2 Miscible Displacement for Extra High Water Cut Reservoir in Xishanyao Formation of Block Cai 9

Zhang Yanmei1, Wan Wensheng1, Li Chen1, Luo Hongcheng1, Liu Yantong2, Zhang Huili1, Zhang Ruixue1   

  1. 1. PetroChina Xinjiang Oilfield Company, Fukang, Xinjiang 831511, China;
    2. Xinjiang Xinyitong Petroleum Technology Co., Ltd., Karamay, Xinjiang 834000, China
  • Received:2020-11-17 Revised:2021-09-22 Online:2021-12-25 Published:2022-02-16

摘要: 目前彩南油田彩9井区西山窑组已进入高含水低产低能阶段,开井率仅为23.0%,即将面临废弃停产。为了提高该井区特高含水油藏产能,降低含水率,利用类比法、油藏工程及数值模拟方法,对彩9井区西山窑组油藏开展CO2混相驱可行性论证及油藏工程设计,并进行先导试验。结果表明:先导试验区应选择小井距反七点井网的C2576井组,注入层位选择剩余油富集的J2x12-2小层,合理注入量为0.3倍孔隙体积(地面CO2注入量为10 500 t),注气速度为30~40 t/d,注采比为1.1~1.2。现场试验证实,该井组累计注入4 529.7 t CO2后,累计增油达到1 269 t,CO2换油率达到0.27 t/t,取得了较好的增产效果。该研究可为彩南油田CO2混相驱扩大试验和全面调整开发提供技术支撑。

关键词: CO2混相驱, 特高含水油藏, 油藏工程, 提高采收率, 彩南油田

Abstract: At present, the oil reservoir in Xishanyao Formation in Well Block Cai 9, Cainan Oilfield is high in water cut and low in production, with a well development rate of only 23.0%, and it will be abandoned and shut down. In order to improve the productivity and reduce the water cut of the ultra-high water-cut reservoir in this well block, analogy method, reservoir engineering and numerical simulation method were employed to analyze the feasibility of CO2 miscible displacement, develop reservoir engineering design, and perform pilot test. The results showed that Well Block C2576 in inverted seven-spot pattern with small spacing was selected as the pilot test area, Sublayer J2x12-2 rich in remaining oil was selected as the injection layer, the reasonable injection rate was 0.3 times the pore volume (the CO2 injection rate on ground was 10 500 t ), the gas injection velocity was 30-40 t/d, and the injection-production ratio was 1.1-1.2. The field test proved that after 4 529.7 t CO2 injected cumulatively into this well block, the cumulative oil increase reached 1 269 t, and the oil displacement efficiency was 0.27 t/t after CO2 injection, achieving a good stimulation effect. This research provides technical support for the pilot test, overall adjustment and development of CO2 miscible displacement in Cainan Oilfield.

Key words: CO2 miscible flooding, ultra-high water-cut reservoirs, reservoir engineering, enhanced oil recovery, Cainan Oilfield

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